Axle Hung
Traction Motor
Intro.
I'm modelling BR
3rd rail electrics in P4, my chosen period is
around
the time of the Bournemouth electrification. I was never happy with the
old
"pancake" type motor bogies and a big motor inside the coach was even
less appealing. What I wanted was to get away from the worm drive and
the motor shaft at 90 degrees to the axle. I also wanted the same
number of motors per unit as the prototype, i.e. 2 car unit 2 motors, 4
car unit 4 motors. I first toyed with the idea of using small Mashima
motors axle hung but this would be expensive and far too powerfull. It
was two things that helped me down this route. Ted Scannell of CLAG
built an axle hung traction motor using a belt drive. I did some
sketches with belt drives but wasn't entirely happy with the
arrangement. I wanted to make it more compact. It was browsing the NWSL
web site that I found something called a "Magic Carpet" for 0 scale
American street cars. This used a small can motor with a plastic
housing and a three stage gear train. This was what I was looking
for.
The Motor
Blocks.
The
original intention was to use cast iron. The
reason for this was the motor block would act as a bearing for the
axle, and it
would act as a heatsink for the motors. An early prototype was made in
iron, but all I have available is rough offcuts and there was a
lot of work required to get it square and to size. A change to steel
was made because it
is readily available in sizes that suit the motor block, which is
12.7mm square by 8mm thick. Brass
bearings are fitted and protude to fix the wheel back to back. The
block on the right has been fitted with motor which is a Nigel Lawton
Micro Motor. These motors measure 6.03mm in diameter, so a 6mm hole is
far too small, and a custom reamer had to be made. This was after the
first one was opened out with a file, and the commutator was push out
the back of the motor.
The Gears

These gears are
made by Didel
in Switzerland. The
pinion is a 12t and has to be cut in half. The two spur gears are
36/12t, and the 12t has to be reduced in thickness, with one of the
bores being opened out to suit suit the axle diameter. The final drive
gear is a 36/12t with 12t cut off and secured to an Alan Gibson wheel
and pin point axle with 14BA countersunk
screws.
Assembled and ready for testing.

The
brass bearings are 3mm long
to reduce friction. and the clearances are very tight. Too loose
and everything wobbles around with the risk of the gears becoming
displaced and jamming. The motor shaft is only just clear of the
wheel back. Too tight and the motor would be severly overloaded. This
view shows the Gibson wheels before the backs were faced flushed.
Testing under power.

Running
at the full 6 volts before any grease was
applied. The second motor was greased on assembly. They were briefly
run
up to 12 volts, just to see what happened. They run faster and didn't
get much warmer. This testing also gave a bit of running in which
reduced the starting voltage. After prolonged running at 6 volts the
motor blocks were just warm, which was very encoraging as it showed
that the heat-sinking of the block was working. When I received
my first two motors I ran
one at 6 volts and held the motor in my fingers, it got a lot hotter
than this set-up.
The Motor Bogie

Two motors assembled
in a heavily modified Masokits
pinpoint bogie. The
motors are wired in series for testing and fitted with temporary
pick-ups. Load testing will use a Bachmann Mk1 using DC power. It is
intended to carry out full testing using an Ian Kirk 2 Bil set, DCC and
live axle/bogie pick-up. I'm going to try a parallel/series switching
arrangement using a function and relay on the DCC.
Load Test.
Under a
Bachmann Mk1 for load testing. All my coaches are fitted
with Masokits pinpoint bogies so they are a straight swap, hence
the temporary pick-ups. The bogie was quite happy moving this coach and
another Bachmann Mk1. Control was very good, with slow running and a
reasonable top speed. It was a little noisey but this is
possibly because one of the final drive gears is slightly eccentric. A
drilling jig will need to be made to correct this. Also it was found
that the motor pinnion on the same unit wasn't in full engagement with
it's spur gear. A minor adjustment to the motor in the block fixed
this.
Graham Hickson
gray@ukfsn.org